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Motiva Enterprises (1406), Norco

Releases of Nitric Oxide

LDEQ Accident Number
Accident Date
Point Source(s) Notes Amount of Release
121572

2010-02-17
FLARE - HCU Elevated Flare [EPN4-84], Relief Valve [RV1178 & RV1204]
Cause: Loss of electrical breaker powering most of the large motors in the hydrocracking unit caused two columns to "release to atmosphere;" RV-1178 on the Rectified Absorber Column for 30secs, RV-1204 on the Caustic Water Wash column "momentarily." FLARE.

Followup: Yes

Notes: BRQ. Refinery Follow-up Letter states "final calculations confirm that no reportable quantities were exceeded as a result of this release." Breaker loss discovered & repaired, operations returned to normal.
134190

2011-09-26
8-84 RCCU Elevated flare
GO-1 Elevated Flare
Cause: On 9/26/11, Motiva's RCCU Process Unit identified smoke exiting the insulation on the process unit's reactor stripper overhead piping, indicating a leak of hydrocarbon. Consequently, the RCCU process unit had to divert feed causing flaring to occur at the RCCU Flare (EPN 8-89). The process unit safely diverted feed and continued to maintain catalyst circulation in order to avoid additional flaring. All operational and safety procedures were following at this time. Immediately after stabilizing the unit, insulation was removed from the overhead piping to determine the source of the leak. the leak was identified as a set of flanges on the reactor stripper overhead piping. Attempts were made to re-torque the flanges and stop the leak. However, the re-torquing efforts were unsuccessful and a decision was made to fabricate and install a blade clamp to permanently stop the leak. As of 9/28/11, the blade clamp was installed and the leak on the overhead piping had stopped. The RCCU had been restarted following all operational and safety procedures and remained at steady operation. the RGHT had not been restarted at that time. On 9/26/11 Motiva Enterprises LLC RCCU unit was shut down to do some maintenance work. Flaring occurred at the GO-1 Elevated Flare (EPN 9-84) as a result of the restart of Motiva's RCCU Unit. Untreated dry gas from the RCCU is flared during the restart of the RCCU at the GO-1 Elevated flare before the dry gas can be introduced to GO-1 as a feed.

Followup: Yes

Notes: The RCCU diverted feed and continued to maintain catalyst circulation in order to avoid additional flaring and stabilize the unit. Operations worked to identify the source of the leak and made preparations for repair. The flanges associated with the leak source were re-torqued in an attempt to stop the leak. A box clamp was fabricated and installed to encapsulate and stop the leak. Maximum lb/hr limits were exceeded for sulfur dioxide and VOC's, because the incident release was spread out across close to 3 days no reportable quantities were exceeded. Two follow up letters were received.
528.3 pounds
134190

2011-09-26
8-84 RCCU Elevated flare
GO-1 Elevated Flare
Cause: On 9/26/11, Motiva's RCCU Process Unit identified smoke exiting the insulation on the process unit's reactor stripper overhead piping, indicating a leak of hydrocarbon. Consequently, the RCCU process unit had to divert feed causing flaring to occur at the RCCU Flare (EPN 8-89). The process unit safely diverted feed and continued to maintain catalyst circulation in order to avoid additional flaring. All operational and safety procedures were following at this time. Immediately after stabilizing the unit, insulation was removed from the overhead piping to determine the source of the leak. the leak was identified as a set of flanges on the reactor stripper overhead piping. Attempts were made to re-torque the flanges and stop the leak. However, the re-torquing efforts were unsuccessful and a decision was made to fabricate and install a blade clamp to permanently stop the leak. As of 9/28/11, the blade clamp was installed and the leak on the overhead piping had stopped. The RCCU had been restarted following all operational and safety procedures and remained at steady operation. the RGHT had not been restarted at that time. On 9/26/11 Motiva Enterprises LLC RCCU unit was shut down to do some maintenance work. Flaring occurred at the GO-1 Elevated Flare (EPN 9-84) as a result of the restart of Motiva's RCCU Unit. Untreated dry gas from the RCCU is flared during the restart of the RCCU at the GO-1 Elevated flare before the dry gas can be introduced to GO-1 as a feed.

Followup: Yes

Notes: The RCCU diverted feed and continued to maintain catalyst circulation in order to avoid additional flaring and stabilize the unit. Operations worked to identify the source of the leak and made preparations for repair. The flanges associated with the leak source were re-torqued in an attempt to stop the leak. A box clamp was fabricated and installed to encapsulate and stop the leak. Maximum lb/hr limits were exceeded for sulfur dioxide and VOC's, because the incident release was spread out across close to 3 days no reportable quantities were exceeded. Two follow up letters were received.
902.3 pounds
134097

2011-09-21
8-84 RCCU Elevated flare
Cause: On 9/21/11, Motiva's SBA Feed Prep Process Unit experienced a block valve malfunction during a back flush of exchanger E-809D. A cooling water supply valve for this exchanger failed in the closed position causing the exchanger to leak for five minutes. Consequently, there was not adequate cooling water to the exchanger and the SBA process unit had to be shutdown and depressured to the RCCU Flare (EPN-8-84). The process unit was safely shutdown following all operational safety procedures. The elevated flaring associated with the shutdown activities stopped on 9/21/11 at 11:15pm. Repair work for the cooling water system was completed and the SBA Feed Prep Unit was successfully restarted on 9/21/11.

Followup: Yes

Notes: The feed to the SBA Unit was immediately diverted and the process unit was idled. Due to a lack of cooling water, the SBA unit was then depressured and the unit cooling water system was de-inventoried in order to make the necessary repairs. Motiva replaced the cooling water valves associated with the system in order to prevent a similar recurrence. The maximum lb/hr permit limits for sulfur dioxide and VOCs were exceeded during the unit shutdown and restart activities.
399.9 pounds
152971

2013-12-23
RCCU Elevated Flare
Cause: On December 23, 2013, the Residual Catalytic Cracking Unit (RCCU) Elevated Flare exceeded its 162 ppm three-hour rolling average limit for hydrogen sulfide. The monitoring capabilities of the hydrogen sulfide analyzer at the RCCU Elevated Flare were exceeded as the hydrogen sulfide to the flare continued to increase. Several contributing factors were identified. One of these factors was that the cold weather was affecting some of the valve bodies by allowing small quantities of H2S to leak through a closed valve during lower ambient temperatures. In addition, it was found that the RCCU flare knock out drum and the maintenance drop out drum were contaminated with H2S as a result of recent shutdown activities. This event did not result in an emergency condition. There were no fatalities, injuries, or road closures.

Followup: Yes

Notes: Immediately, Operations began a systematic search for the sources of H2S routed to the flare. This search identifies all potential H2S intrusion points with the RCCU and RGHT Units, and prioritized those most likely contributing to the elevated H2S in the Flare system. Flushes the RCCU Elevated flare knock out drum and the maintenance drop out drum. Upgraded valves HV4346 a IV one-piece metal seats to class VI three-piece metal Teflon seats. Unit rate increases were delayed and unit feed rates were maintained during the duration of the incident. To prevent recurrences, the refinery will (1) evaluate the need to upgrade/replace additional RV and HIC valves that are routed to the RCCU Elevated Flare header in order to prevent leakage during cold weather; and (2) evaluate the need to apply weather shields and/or steam lances to valves affect by cold weather. The report does not mention when the refinery will implement these preventative measures.
1.9 pounds
152855

2013-12-14
RCCU Flare (EPN 8-84)
RCCU Flare (EPN 8-84)
Cause: On December 14, 2013, the three-hour rolling average for the amount of hydrogen sulfide to the Residual Catalytic Cracking Unity (RCCU) Flare exceeded its 162 ppm limit. The hydrogen sulfide to the RCCU Flare continued to increase exceeding the monitoring capabilities of the flare's hydrogen sulfide analyzer. As a result, Operations monitored the hydrogen sulfide concentrations by sampling the flare header. Hydrogen sulfide concentrations fluctuated as troubleshooting occurred. Several contributing factors were identified. One of these factors was that the cold weather was affecting some of the valve bodies by allowing small quantities of H2S to leak through a close valve during lower ambient temperatures. In addition, it was found that the RCCU flare knock out drum and the maintenance drop out drum were contaminated with H2S as a result of recent shutdown activities.

Followup: Yes

Notes: Immediately, operations began a systematic search for the sources of H2S routed to the flare. This search identified all potential H2S intrusion points within the RCCU and RGHT Units, and prioritized those most likely contributing to the elevated H2S in the Flare system. Next, they flushed the RCCU elevated flare knock out drum and the maintenance drop out drum. Unit rate increases were delayed and unit feed rates were maintained during the duration of the incident. To prevent recurrences, the refinery will evaluate the need to upgrade/replace additional RV and HIC valves that are routed to the RCCU Elevated Flare header in order to prevent leakage during cold weather. Additionally, it will evaluate the need to apply weather shields and/or steam lances to valves affected by cold weather. Note: the 60-day report states: "Data gathering and calculations confirm no reportable quantities were exceeded during the release. However, the maximum pound per hour permit limit for sulfur dioxide was exceeded during this incident," and "The hydrogen sulfide to the the RCCU Flare exceeded the monitoring capabilities of the flare's hydrogen sulfide analyzer." Hence, the amount of hydrogen sulfide released (and not oxidized to SO2) is unknown.
19.8 pounds