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Calcasieu Refining (3585), Lake Charles

Releases in 2013

LDEQ Accident Number
Accident Date
Point Source/Release CauseNotes
151176

2013-09-21
Point Source(s):
No Information Given

Pollutant(s):
Unknown Liquid - BRQ
Cause of Problem: No Information Given

Cause is Unknown. An approximate 20' x 5" sheen was discovered at the end of the Calcasieu Refining Outfall Ditch. The facility had 8.10" of rainfall in less than 24 hours which could have resulted in some runoff leaving the facility and being the possible source of the sheen.
The hydrocarbon creating the sheen was unrecoverable. This incident will be discussed during this facility's next compliance evaluation inspection. On 9/21/13 at 14:16, an incident was reported to the National Response Center concerning a sheen in the Calcasieu River. The incident was reported by Don Johnson, Calcasieu Refining Environmental Manager. An approximate 20' X 5" sheen was discovered at the end of the Calcasieu Refining Outfall Ditch. According to Mr. Johnson, the facility had 8.10" of rainfall in less than 24 hours which could have resulted in some runoff leaving the facility and being the possible source of the sheen. The hydrocarbon creating the sheen was unrecoverable. This incident will be discussed during this facility's next compliance evaluation inspection. No refinery letter from the Calcasieu Refining Company was located by LABB as of 2/10/2014.
149327

2013-06-20
Point Source(s):
transfer hose

Pollutant(s):
Crude Oil - 210 gallons
Cause of Problem: Piping or Tubing

At approximately 3:25 PM on June 20, 2013, a barge unloading hose ruptured during off loading of crude oil from a barge at Calcasieu Refining Company C-Dock. This occurred when a strong wake from a deep draft ship pulled the barge away from the dock far enough to stretch and rupture the hose. Original estimate of release was 10 barrels, but actual release was 5 barrels.
The substance released did escape beyond the incident location affecting the waters of the Calcasieu River. Immediate action by CRC personnel was to hit emergency shut off devices which minimized the amount of oil discharged and deployed two spill boats and 2500-3000 feet of containment boom. Oil recovery was accomplished using sorbent pads and sorbent boom material. Approximately 22 cubic yards of soiled absorbents were recovered and will be properly disposed of. An emergency response plan was in place and initiated by Enterprise Marine Services LLC. The spill response was a shared responsibility between Enterprise Marine Services LLC and the Calcasieu Refining Company. The owner/operator of the M/V Princimar Hope (ship responsible for causing the wake) has been put on notice. An OSRO crew from ES&H Consulting Services, Inc was contracted to conduct remedial activities. No information is given about whether release was below reportable quantity, but final estimated amount released (5 barrels) is greater than reported quantity for crude oil (1 barrel).