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Alon Refining (3116), Krotz Springs

Releases of Nitrogen Dioxide

LDEQ Accident Number
Accident Date
Point Source(s) Notes Amount of Release
117771

2009-09-04
flare
Cause: Crude unit upset resulted in intermittent flaring from 3 different process vessels.

Followup: No

Notes: Reduced rates and shutdown isomerzation and LRU unit to minimize flaring until flow rates could be stabilized. Same issue as the release on the previous day.
11.2 pounds
117731

2009-09-03
flare
Cause: Crude unit upset caused flaring from 3 different process vessels.

Followup: No

Notes: Reduced rates and shutdown isomerzation and LRU unit to minimize flaring until flow rates could be stabilized.
23.3 pounds
127252

2010-10-25
FLARE - FCCU flare
Cause: "Loss of power in Complex II caused operating and utility units to shutdown. This even resulted in flaring from the FCCU flare" Due to the loss of power, the complex II steam producers shut down, therefore the flare steam assist was lost. This resulted in smoking flares. This released the following chemicals: SO2, H2S, NOx, VOC, Hexane, and 1,3 Butadiene. FLARE.

Followup: No

Notes: A power feed was connected from Complex I to Complex II, and boilers were restarted to produce steam to assist the FCCU flare, and shutdown procedures was continued. No LDEQ report. Refinery Letter only.
1.7 pounds