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LDEQ Accident Number Accident Date |
Point Source(s) | Notes | Amount of Release |
No LDEQ Reported 2007-10-14 | Fin Fan Leak in Poly Unit | Cause: xxxxxxxx Followup: no Notes: Need to find LDEQ #. A small leak was discovered in the Fin Fan in the Poly Unit so the unit was shut down immediately. It re-opened 10/18/2007. All the tubes were re-rolled and then hydrotested for additional leaks and none were found. | Butane: 979.0 pounds |
99248 2007-09-07 | Fin Fan Leak in Poly Unit | Cause: xxxxxxxx Followup: no Notes: A small leak was discovered in the a tube of a Fin Fan in the Poly Unit so the unit was shut down immediately. It re-opened 09/08/2007. The tubes were hydrotested for additional leaks and none were found. | Butane: 730.0 pounds |
99045 2007-08-16 | Leak in tube of Poly Debutanizer Overhead Fin Fans in Poly Unit | Cause: xxxxxxxx Followup: no Notes: A pin-hole sized leak was discovered in the a tube of a Poly Debutanizer Overhead Fin Fan in the Poly Unit so the unit was shut down immediately It re-opened 08/11/2007. It was shut down again on 8/14/2007 to replace the bundle of tubes. | Butane: 337.0 pounds |
98022 2007-07-20 | Fin Fan Leak in Poly Unit | Cause: xxxxxxxx Followup: no Notes: A pin-hole sized leak was discovered in the Fin Fan in the Poly Unit so the unit was shut down shortly after. It re-opened 07/21/2007. | Butane: 211.5 pounds |
97619 2007-07-05 | Fin Fan Leak in Poly Unit | Cause: xxxxxxxx Followup: no Notes: A pin-hole sized leak was discovered in the Fin Fan in the Poly Unit so the unit was shut down. It re-opened 07-07/2007. | Butane: 192.3 pounds |
117771 2009-09-04 | flare | Cause: Crude unit upset resulted in intermittent flaring from 3 different process vessels. Followup: No Notes: Reduced rates and shutdown isomerzation and LRU unit to minimize flaring until flow rates could be stabilized. Same issue as the release on the previous day. | Volatile Organic Compounds (VOCs): 381.4 pounds Nitrogen Oxide: 101.0 pounds Nitrogen Dioxide: 11.2 pounds Carbon Monoxide: 224.2 pounds Benzene: 18.6 pounds n-Hexane: 133.6 pounds |
117731 2009-09-03 | flare | Cause: Crude unit upset caused flaring from 3 different process vessels. Followup: No Notes: Reduced rates and shutdown isomerzation and LRU unit to minimize flaring until flow rates could be stabilized. | Volatile Organic Compounds (VOCs): 477.9 pounds Nitrogen Oxide: 209.7 pounds Nitrogen Dioxide: 23.3 pounds Carbon Monoxide: 465.2 pounds Sulfur Dioxide: 0.4 pounds n-Hexane: 275.2 pounds Benzene: 38.4 pounds |
116654 2009-07-22 | Boiler stack | Cause: While turning the Boiler B-8203, the contractor identified potential burner problem that could be causing a small amount of uncombusted fuel gas to be flowing through out the stack with the combusted fuel gas. Followup: No Notes: Cut back boiler and steamed burners to attempt a fix, with limited success. Shut down boiler and repaired burner. | Gas Oil: 9,438.5 pounds Hydrogen Sulfide: 0.8 pounds Volatile Organic Compounds (VOCs): 700.8 pounds |
No LDEQ Reported 2012-09-20 | Valve Bonnet and Flange on Dock #3 transfer system (EQT 062: 23-79) | Cause: LCO drip into Atchafalaya River from valve bonnet and flange on transfer system at Dock #3 (EQT 062: 23-79). Followup: No Notes: Location of drip identified. Washed bonnet, flange, and areas affected. Associated component bolts were tightened to stop the leak. Boom was placed in the river. | Light Cycle Oil: 4.0 pounds |
155791 2014-03-07 | Piping at demineralization skid | Cause: Automatic isolation valve failed during sulfuric acid injection cycle of water demineralization resin regeneration, allowing sulfuric acid to flow through vent to containment with some reaching the ground. Followup: No Notes: Spilled product was contained, equipment isolated, and affected areas were remediated. Report states that estimated release of sulfuric acid was 3200 lbs, estimated quantity recovered was 8000 lbs. | Sulfuric Acid: 3,200.0 pounds |
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